I've just finished installing my new multi function relief valve.
I made a mounting plate for it and bolted that plate up to the right hand frame rail, right behind the place where the loader cross-member will bolt in, and detached the power steering valve's return-to-tank hose from where it used to attach to the return-to-tank manifold right near the hydro oil filter, and routed that hose down and attached it to the new multi-function relief valve. Then I created a new 3/8 hard line that runs from the new multi-function valve up to the now open port on the return-to-tank manifold.
Next I made the plug that's needed to seal off the accessory lift relief valve inside the TCV. The inner hole where the relief spring fits is 3/8". So I made the plug a few thousandths less than that, and gave it an o-ring groove, and put a 3/8" o-ring in the groove.
I decided I wanted the plug to be somewhat "captive" to the 7/16-20 threaded outer plug. So I made a new outer plug on the lathe and drilled a 3/6" hole about halfway into its depth. Then I turned a 3/16 journal on the end of the 3/8" inner plug that slides up into that hole. That way everything stays in straight alignment as you push/screw it in. I used a bandsaw to cut flat-tipped screwdriver slot in the end of the threaded outer plug.
Everything screwed in without any drama, though it was fairly tight. I'm not certain, but the o-ring may have hung up on internal obstacles and gotten cut. Time will tell when I pressure test it. The steel of the plug itself is also screwed tight into the beveled seat, so the o-ring may not really matter that much anyway. As long as I can get full 2000 psi+ at the point of my new spool valve, I'm happy.
Meanwhile, I needed to install two new tees to connect from the work ports on the accessory lift over to the new relief valve. I put the first tee into the line that currently has a single output line, a line that leads up to the selector valve. That tee went in without too much drama, though I had to do some creative bending to get the 3/8" hard lines bent/squeezed/looped in the tight space. 5/16" tubing is a lot easier to work with, but JIC 5 fittings are expensive and hard to find, so I just went with JIC6 and 3/8" tube.
The second tee goes into the the other work port line, and that already has one tee installed, since it's connected to both the mid lift cylinder and the 3 pt. cylinder.
But when I put a tee on there that situation goes from unwieldy to ridiculous. Converting from JIC 5 to 6, converting from JIC to NPT, it's just not the way I want to leave it.
So I chucked up some 1" round bar and turned into a 4-way tee/mini manifold. It's just simple drilling and tapping.
After it's installed, it's not amazing looking, but it's better than it would have been otherwise. I had to make a full-on s-tube to get it joined. I'm sure it could be routed better and cleaner, but it's not obvious how, at least to me.
You may notice I use teflon tape on these NPT fitting, and I know that's somewhat controversial. I am very careful to never wrap the teflon on the very tip of the fitting, so that no teflon can ever squeeze down into the flow chamber itself. All the tape remains within the space between the threads.
Next I fill it all back up and do pressure testing and adjusting. But that'll probably be tomorrow.
Bob